地铁隧道内钢弹簧浮置板轨道的减振效果实测分析
黄俊飞1秦佳良2
On-site Measurement and Analysis of Vibration Reduction Effect of Steel Spring Floating Slab Track in Metro Tunnel
HUANG JunfeiQIN Jialiang
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作者信息:1.隔而固(青岛)振动控制有限公司,266108,青岛;
2.华东交通大学土木建筑学院,330013,南昌
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Affiliation:GERB (Qingdao) Vibration Control Co., Ltd., 266108, Qingdao, China
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关键词:
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Key words:
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DOI:10.16037/j.1007-869x.2020.01.020
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中图分类号/CLCN:U213.2+42;U211.3
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栏目/Col:研究报告
摘要:
为了研究地铁隧道内浮置板轨道的实际减振效果,以我国某地铁线路的隧道段为研究对象,测试了普通道床轨道、重量级和中量级浮置板轨道产生的振动响应,分别在时域和频域内对各种轨道的振动特性进行对比分析,并采用Z振级进行综合评价,结果表明:轨道板和隧道壁的主要响应频段在80 Hz附近;重量级和中量级钢弹簧浮置板道床振动响应有5.3 dB的差异;各减振断面的隧道壁振动均满足相关规范的要求。
Abstracts:
In order to study the actual vibration reduction effect of floating slab track in metro tunnel, a tunnel section on metro line in China is taken as the research objective. The vibration responses of ordinary track bed, heavyweight and medium-sized floating slab track are tested within a certain domain of time and frequency, the vibration characteristics of various tracks are compared and analyzed, and the Z vibration level is adopted for a comprehensive evaluation. The results show that the main response frequency bands of track slab and tunnel wall are near 80 Hz; the vibration response of floating slab bed of heavyweight and medium-weight has a 5.3 dB difference, the vibration of tunnel wall of each vibration reduction section could meet the requirements of relevant codes.
引文 / Ref:
黄俊飞,秦佳良.地铁隧道内钢弹簧浮置板轨道的减振效果实测分析[J].城市轨道交通研究,2020,23(1):83.
HUANG Junfei,QIN Jialiang.On-site Measurement and Analysis of Vibration Reduction Effect of Steel Spring Floating Slab Track in Metro Tunnel[J].Urban mass transit,2020,23(1):83.
HUANG Junfei,QIN Jialiang.On-site Measurement and Analysis of Vibration Reduction Effect of Steel Spring Floating Slab Track in Metro Tunnel[J].Urban mass transit,2020,23(1):83.
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